Tech Tips

The Spoke Wheel Dilemma
Part Two
"Going Tubeless"
By: Larry Diaz

     In the first part of "The Spoke Wheel Dilemma," I addressed the problem of wheels that seemed impossible to balance and the efforts made to come up with a smooth ride.

    My next goal is to make my spoke wheels accept tubeless tires without inner tubes. For most of us, it has been quite a while since we have had to deal with tube tires. I was talking with a friend and we seem to remember that the tubeless tire became standard in the middle sixties. For most of us it has been around thirty-five years since tube tires. We tend to forget the headaches involved with them.

    Flats are a bigger problem with tube than with the tubeless. If you have a flat tire with a tubeless tire, the tire is simply plugged, pumped up to proper P.S.I. and you are on your way. If you have a flat with a tube, it becomes more bothersome. The tire must be taken off the rim for the repair to take place. For those with the spoke wheels, the process of taking the tire off the rim adds wear and tear to the rim. With the use of pneumatic tire changers, the likelihood of warping or bending the rim is even greater. The tube must be patched and reinserted into the tire. Thirty-five years ago any service station attendant possessed the skills and knowledge to deal with tube flats. As time has gone by, these skills and the knowledge of repairing a tube tire is not as easy to come by. If and when you get the tube repaired and replaced in the tire, then comes the added expense of re-balancing the tire. If you are lucky enough to find a repairman who still processes the skill, he would have remembered to mark the tire as it came off the rim along with the lead attached to the rim thereby saving the expense of re-balancing.

    Another problem with the tube tire is the tube itself. In the sixties there just were not that many tire sizes. There were the standard 13, 14, and 15-inch tire size. Within these sizes there were a few variations but nothing like there is in 2003. Tubes were plentiful for the available tire sizes. This is not the case today. If you can even find a tube that fits, for example, a 14-inch wheel, it will fall within the one-size fits all categories. As a result, you may end up with a 15-inch tube in a 14-inch rim. This will happen because this was the only tube the attendant had to put in your tire. In due time you will have a flat with this arrangement. The reason for the flat is that folds will be in the inner tube. Along the folds a crease will develop just like folding a piece of paper over before you tear it. The crease makes the tube weaker and the result is a hole in the tube. I just had this exact thing happen except instead of one hole, I had four.

    Flats with a tube tire have different characteristic then flats with the tubeless. Once a tube tire starts to go flat, the driver has very little warning before the tire is completely flat. It has been my experience that you have just enough time to make an emergency stop if you are running interstate speed. If you have ever had to do this, you know this is not a safe situation to be in, especially in heavy traffic. A tube tire gives warning. They have a tendency to go slack and the driver can feel the car wobble a bit before all control is lost. I could go on with the advantages of a tubeless tire but I believe the point is made.

            Now about the business of making a spoke wheel tubeless. The problem with making a spoke wheel tubeless is the rim itself. On a MGB like mine, there are sixty spokes that come through the rim. Each place in the rim where the spoke is inserted is a nipple. This area is not an airtight seal. To make things worse, the spoke itself is threaded into this nipple. The treaded spoke into the nipple is not airtight either. In one wheel there are 120 spots for air to leak out. I decided to try to seal these trouble spots. In my first attempt I took a hand wire brush and cleaned the nipple surfaces on the inside of the rim. I had a tube of 100% silicon, the type that goes in a caulk gun, and covered each nipple. I then let it set for a day, put a tire on it and pumped it up. I checked and had 7 leaking spokes. At first I was disappointed, but then I realized that if ever a teacher in school gave me a test with 120 questions on it and I only goofed up on 7, then I was happy (At least I think I would have been because I never achieved that rate of success). I decided to move forward with what now I considered a successful test. I took the tire off the rim and got my side grinder out. I put on a wire wheel and really cleaned it, smeared on the silicon, let it set and pumped it up to 45 PSI.  That was over four weeks ago now and it still has 45 PSI. I am now confident that I can get a tire to hold air just lying around the shop. Going down the road presents a different set of problems. My concern was the sealant might come loose due to vibrating or heat buildup so I decided to change the sealant. I bought a substance with the brand name of Lexel. It has silicon type characteristics but with better adhesion properties. It also had a wider temperature range when applying.

It could be applied in temperatures as cool as 0 degrees Fahrenheit and as hot a 135 degrees Fahrenheit. I thought that once it cured, it would be able to exceed this temperature range. It also can be painted. This helps because once the paint is applied, any area not sealed shows up as not being painted. I also went one step further in the cleaning process. Instead of cleaning with a wire brush, I sandblasted. After sealing with Lexel, I let it set up for three days and put the tire back on the rim. I pumped air into it and have road tested it for fifty miles or so. So far I have not lost any air and it seems to be holding up fine. All I need to happen now is for this to stand the test of time and the heat of summer. My plan called for me to do this one tire and test it throughout the summer driving season that includes extra driving miles complete with road heat. My first real outing was a planned club trip to Maggie Valley, North Carolina after our March club meeting. This trip would have put around one hundred fifty miles on the tires.  Notice I said would have. Not one mile on our planned journey, I had another flat tire. The cause was another fold in the inner tube in one of the three tires that still had tubes in them.  I parked the car at a nearby restaurant, and my wife and I continued the trip with a fellow club member in their Rover. After returning home, I did not bother to repair the inner tube. Instead, I made this wheel tubeless like the other.

    It is now May and my wife and I are going to West Virginia from South Carolina.  I now have two tubeless tires that have held a constant air pressure during the past three months.  I am encouraged because not only has the air pressure held constant for such a long period, it has also included quite a few miles driven locally. I am confident that the tires will not present a problem for us, but just in case, I have two inner tubes in the trunk!

    We have made it back from our West Virginia trip. I am happy to report that in over 900 miles of mountain driving, we did not experience a tire failure. I guess now I can consider this experiment a success and will convert my remaining wheels to tubeless.